Two For One
The 2011 Impala came in
to the shop for a rough idle and P0300 misfire code. The shop determined that
the cause of the concern was throttle body coking. After cleaning the throttle
body the engine had a high idle, around 1700 RPM, and wouldn’t drop, even after
a battery disconnect.
Coking comes from
certain emission control components that capture crankcase oil vapors and small amounts of exhaust
fumes and re-directs them back thru the intake system of the internal
combustion engine. Too much time in stop and go traffic or idling isn’t the
best for an internal combustion engine. This type of driving/operation can
significantly carbon/coke up their engine very quickly. Another bad habit is
hard acceleration. This over fuels the engine and leads to more problems
including more carbon/coking build-up.
“So, how do we bring the idle speed
back down?” Raul asked.
“First, realize that then engine
computer learns the airflow through the throttle body to calculate the correct
idle speed and stores the calculations in its memory.”
“Yeah, but can’t it compensate for
coking?”
“It does,” I explained, “But up to a
point. Then when you cleaned the coking, you changed the throttle body airflow
rate.”
“Right—but doesn’t the engine computer
learn the new values on its own?”
“It may take several drive cycles to
learn out the coking, Raul. But you can also use a scan tool to reset all the
learned values back to zero.”
“My scan tool doesn’t have anything
like that,” he said.
That’s why I brought mine to his shop.
I consulted the service information because the relearn procedures can be
different depending on the vehicle.
“To reset the learned values to zero,
we turn the ignition ON, engine OFF,” I said, finding the Idle Learn Reset
procedure in the Module Setup menu on the scan tool.
“Next, we start the engine and monitor
the throttle idle airflow compensation data PID.” The engine was already idling
normally now and the data PID was at zero, which was where it belonged. I
checked for trouble codes; there were none, and Raul took the vehicle out on a
short road test. He was all smiles when he returned.
“The Impala runs great now.”
That one was easy. But Raul wasn’t
going to let me off that easily.
“Hey, as long as you’re here, Bob, I
have another one for you.”
Here it comes. “What is it?”
“I’ve been fighting with a 2009 C4500
eating up heater cores all the time,” he said. “We did a coolant flush first
and that didn’t fix it. I switched coolants and put a ground on the heater core
but that didn’t help.”
I was writing this all down in my
notepad, of course. The memory isn’t as good as it used to be. “Get rid of the
heater core ground,” I said. Back when electrolysis first cropped up as a
cooling system problem, some technicians tried to re-route stray voltages to
battery ground. But it merely accelerated the problem. I asked what else had
been done to the truck.
“We installed a water shutoff valve to
shut off flow to the heater core when not in use, but we still have issues with
the truck. How about if we install a copper and brass heater core?”
“That would be treating the symptom but
not the disease,” I said.
“We checked for bulletins and other
documents but found nothing.”
I wrote that down. “Did you check for
voltage in the coolant?”
Raul nodded. “A tenth of a volt, maybe
less,” he said. We touched the negative voltmeter probe to battery ground and
pot the positive lead into the coolant. We didn’t touch any metal, either.”
“Did you check for both DC and AC
voltages?” I asked.
Jim, one of the technicians, asked me
why they had to check for AC voltage.
“Keep in mind that you could have a bad
engine block heater or faulty alternator diode,” I explained. “Did you check
all the grounds?”
“They’re all good,” Jim said.
“Let’s check them statically,” I said. “Turn off all accessories. Turn
ignition on, but do not start the engine.” I had them check with the ground
probe of the meter to battery ground, engine ground and vehicle ground,
sequentially. They found one ground connection that needed cleaning. We
continued our testing.
“Check the accessories without
using the on/off switch on the vehicle instrument panel, use a jumper wire to ground,”
I instructed. Next, we turned on all the accessories. We tested again with the
ground probe of the meter to battery ground, engine ground and vehicle ground.
We were coming up with about two-hundred milli-volts.
“The spec calls for .4 volts or
less,” I said.
“Can static buildup cause
problems?” Raul asked.
“Rubber-mounted driveline
components, a squirrel cage spinning in a plastic HVAC case when the blower
motor isn’t properly grounded, and even tires.”
“Tires?” Jim asked.
“Tires?” Raul asked.
“A while back, a certain tire
company got complaints from drivers who kept getting zapped whenever they got
out of their vehicles. The tires were producing a static buildup when the vehicle
was driven under certain conditions.”
“Maybe that’s the problem here,”
Raul offered.
“What’s this truck used for, Raul?”
I asked.
“Deliveries—it’s a delivery truck.”
“Lots of stop-and-start driving?”
“Right,” he said.
“Did you check for coolant voltage
while cranking the engine?”
Bingo.
In cases of electrolysis, a
defective or missing ground on an electrical component causes the electricity
to seek the path of least resistance whenever the component is energized.
Sometimes the path of least resistance is a radiator or maybe a heater hose, or
the radiator or heater core. As the current draw of the poorly grounded
accessory increases, so does the destructiveness of electrolysis. A poorly
grounded engine and starter motor can flow enough current through the cooling
system to blast apart a heater or radiator in a matter of weeks or even days,
depending on how often the vehicle is driven with stops and starts.
It was a long weekend. Closing up
shop.
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